This is filler as I’ve not looked at the news nor anything else on Friday.
As I’m writing this at 1830 on Friday, my hands are almost as grease covered as the worker’s hands in the image. I’ve been up since 0700 and have been at work on the Truck since 0930.
First stop, the auto supply store for cotter pins, brake cleaner, and brake fluid.
The first wheel comes off just fine.
Then it was time to take of the calibers. That is where I got my first surprise, these are big, and they do not float.
I’m used to calibers that are attached to the knuckle with two 14 mm headed screws. Torque specs are “yep, click”.
These bolts are normally greased and the calibers just float on the pin portion.
Not mine. They are attached with bolts torqued to 91 ft/lbs, and they are stuck. It took nearly 45 minutes to break them free using a 1″ black iron pipe as a cheater. The big issue was that there was not enough room to work the breaker bar with cheater. I got it done.
Once the caliber was off the truck, it was time to attack the rotor.
The rotor refuses to leave the truck. I whaled on it with a 5 pound hand sledge, it did not budge.
Second trip out, I sent my son to get some 6mx1.0 jack bolts. He returns with exactly what I needed. It only took three text messages. “What is grade 8?”, “do you want the type with the hex top?”, and “How long do they need to be.
Guess what? They don’t fit.
It is only then that I remembered that I have a nice thread gage checker. This is a steel cable with most thread sizes you would find in normal stuff. Each “key” (my son’s term for them), has an external threaded section on one side and an internal threaded section on the other.
In other words, you can screw one side into a hole, and you can screw bolts and screws into the other side.
Testing the jack boltholes I find they are 8m1.25 Off my son goes to get them.
With those in hand, the rotor comes off,
It is now time to attack the axle dust cap. This doesn’t want to come off, but a gentle (not really) attack with a cold chisel, and it gives me a gap for a pry bar to pry it off.
This revels the first clean metal I’ve seen, the axel, axel nut, and the lock for the axel nut.
With a bit of help from my son to keep the hub from rotating, I apply 300+ foot pounds with my foot. There is a load SNAP and all the tools let go. The bar being used to stop the hub from turning, the breaker bar, the 36 mm socket all went their directions.
We recovered all the pieces. I inspected the axel for damage, trying to figure out what snapped. The axle nut now spins off with just light finger pressure. Good news.
I then get the first “win” of the day. Driving the axel out of the sandpaper, err, bearing, was easy and just worked the way it was supposed to.
Driving the other side off? Not so much. After way too much effort, some stupids along the way, my son and I were able to drive the bearings off the knuckle.
The day is good!
After all that work, it is time to start reassembling the front right side. I picked up the “hub with pressed bearings” and compared it to the old part.
Not only does it not match the old part, I can’t make it work without someway to cut a spline in the damn thing.
I messed up. I wasn’t paying enough attention when I ordered front-wheel bearing assemblies. Yes, it had the 6 lugs, but it turns out that there was another version of the Tacoma which uses the heavy-duty brakes, calibers and all the rest, but it is RWD only.
I’m almost in tears. My son takes me to the parts store. They have it in stock. $195. Rockauto.com sells a better version for $106. OUCH! This is precisely what I was hoping to avoid.
It is too late to got back, I buy the parts and we go back.
With the correct part in hand, we can install the bearing assembly. I was just a question of tightening each bolt in sequence, the same amount.
I even have the right tools to torque the bolts. I’m a happy creature.
Time to install the new rotor.
This is where I started cussing to myself.
As I was checking out, I had the rotors, pads in the cart. The website suggested that I use a kit because it came with more hardware, and it was cheaper.
I went for it.
And missed that I had returned the 6 lug version and replaced it with a 5 lug version.
After a short crying jag, my son takes me back to the parts store. Yes, they have the parts in stock. 2 rotors and a set of pads. But because they only have premium in stock, $214.
The passenger side is completed. The bearing has been replaced, the rotor has been replaced, pads have been replaced, brake caliber has been replaced.
The only thing remaining is bleeding the brakes.
Starting work on the driver’s side. The damn wheel won’t come off the rotor! This required energetic use of that five pound sledge with a long punch to knock it off the rotor.
Jack bolts and a bit of hammering and the rotor came off. The brake caliber is stuck on and the head of the bolt holding the hard line on the hub side and the flex line on the frame side rounds over. I can’t get it off.
My son bounces on the breaker bar a few times before the bolts finally come loose. We managed to get the correct two bolts out, pay no attention to the extra bolt we took out.
We then got the hub ready for the new rotor. It took 30 minutes to get the rotor and caliber installed. It was then that I noticed that the hard line doesn’t line up. I take the top bolt out of the caliber and attempt to get the hard-line to attach.
That is when I called it. I was afraid I was cross threading the hard line to the caliber.
I’m tired, I’m grumpy, I don’t want to see the crap and noise that the leftist put out today.
I hope you are having a great weekend. I’m out there working on the truck. Only about 4 hours more of work.
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